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We believe
corrective action programs offer the best window into assessing whether
nuclear plants have effective operational and safety programs in place.
Corrective action programs should not only assist with problem
identifications; they should identify and resolve the root causes of the
problems that are identified. These programs constitute the largest portion
of the NRC's baseline inspection regimen.
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The mere
fact that in some cases NRC inspectors, rather than plant employees,
identify problems that go into the corrective action program doesn't mean a
safety problem exists. Some problems that are identified have more to do
with ?compliance? with regulatory requirements that were put on the books
decades ago than they do with safety. What matters at the end of the day is
whether the corrective action program is effectively determining and
resolving the root causes of these issues, regardless of whether they relate
to safety or compliance.
AEP's Cook Nuclear Unit 2 Sets Record.
American Electric Power's (NYSE: AEP) Cook Nuclear
Plant Unit 2 set several fuel cycle records as the reactor was safely shut
down early Saturday to begin a refueling outage.
Unit 2 operated continuously since the last refueling in spring
of 2006 for a site record run of 497 days. This is known in the industry as a
breaker- to-breaker run, as the unit's circuit breakers remained connected to
the transmission grid for the entire 18-month fuel cycle. Projected totals
show the unit operated at 100.6 percent capacity factor, a record for Unit 2
and equal to Unit 1's best performance, and generated 12,903 gigawatt -hours
(GWH) of electricity, just shy of the Cook site record of 13,224 GWH which
occurred during a longer fuel cycle.
MY comments: Compare this to that of
solar PV's which have capacity factors of 15% and wind power with
CF of 20%. Which energy system will win out in the long run?
DETERRING
TERRORISM:
Aircraft Crash Impact Analyses Demonstrate Nuclear Power Plant’s Structural
Strength
Conclusion
The study determined that
the structures that house reactor fuel are robust and protect the fuel from
impacts of large commercial aircraft.
For more information
on nuclear power plant security and other industry issues, contact the
Nuclear Energy Institute at 202.739.8044 or www.nei.org.
NEI Says Many Safety Indicators Show Record-Best Levels
of Excellence at Nuclear Power Plants in 2006
WASHINGTON, Apr 30, 2007 -- BUSINESS WIRE
America's nuclear power plants continued to operate at
high levels of efficiency and safety in 2006, according to industry
performance indicators compiled by the World Association of Nuclear Operators.
For the seventh consecutive year, the U.S. nuclear energy
industry's unit capability factor topped 90 percent. The median capability
factor for 103 reactors of 91.5 percent, when measured on an operating cycle
basis, was within four-tenths of a percentage point of the 91.9 percent record
set in 2005. Unit capability factor is the percentage of electricity actually
produced compared to the maximum electricity a plant could supply to the
electrical grid.
These sector-leading levels of efficiency at nuclear
power plants produced 787.2 billion kilowatt-hours (kwh) of electricity last
year, second only to the record-high of 788.5 billion kwh of electricity
produced in 2004.
The nuclear energy industry similarly sustained
excellent levels of safety and operating performance in areas including safety
system performance, industrial safety, unplanned automatic reactor shutdowns,
and programs to protect workers from radiation exposure.
"The 2006 performance indicators are another indicator
of the nuclear industry's commitment to safety and efficient operations," said
Frank L. "Skip" Bowman, the Nuclear Energy Institute's president and chief
executive officer. "As our industry prepares to build new state-of-the-art
nuclear plants, it's noteworthy that we move forward from a solid foundation
of operating excellence at our existing plants."
The performance data compiled by WANO is analyzed by the
Atlanta-based Institute of Nuclear Power Operations, which promotes excellence
in U.S. nuclear power plant safety and operations. INPO uses the data to help
set challenging benchmarks of excellence against which safety and plant
operation can be measured.
PG&E's Diablo Canyon Power Plant Begins Scheduled
Refueling and Maintenance Outage On Unit 1
AVILA BEACH, Calif., April 30, 2007 /PRNewswire
Diablo Canyon Power Plant operators safely shut down
Unit 1 at 1:30 a.m. Monday, April 30, 2007 to begin a scheduled refueling and
maintenance outage. Unit 1 operated continuously for 513 days, beginning at
the conclusion of the last refueling outage in December 2005.
"Operating Unit 1 continuously between refueling outages is a
testament to the people who maintain and operate it safely and efficiently
every day," said Jim Becker, Vice President, Operations, and Station Director.
"The Diablo Canyon team is prepared to execute a world-class outage that will
set the stage for another long, continuous run for our customers."
Diablo Canyon personnel, supplemented by over 1,200
specialized and local union contractors, will complete nearly 11,000 tasks
during the outage, including replacing one-third of the nuclear fuel. This
will allow the plant to produce electricity safely and efficiently through the
next 18-month cycle.
Diablo Canyon's two units together produce 2,300 net
megawatts of electricity, about 10 percent of all electricity generated in
California, and enough to meet the needs of over 2 million homes in central
and northern California.
SOURCE Pacific Gas and Electric Company
My comment: Can you believe a full power
run of 513 days or 1.4 years?.
Diablo Canyon can now again operate
at fill power for another year and a half. This will be a capacity factor of
about 90%. Compare this to wind power machines that can operated at capacity
factors of only 25%.